[Drake] Drake L4B/8877 Retrofit
[email protected]
[email protected]
Sun, 2 Jun 2002 18:52:24 -0400
It appears that the Yahoo site I was planning to use in order to share
the details of the retrofit is not going to work for me. I put the
annotations in plain text (below) If you need the the deck and power
supply digitals, I'll send them the "old fashioned way" 73's Ron W2CQM/3
Drake L4B/8877 Retrofit
Part I
Work has begun in earnest preparing the Drake L4B for its rejuvenation
and reintroduction into the new century. My prologue, appearing on the
Reflector a while back, announcing the initial phase of the project also
suggested most strenuously to the Drake Reflector constituency that the
(anticipated) bad mouthing, and those espousing my alleged guilt of
heresy need not respond. I�ve been through that gauntlet as a result of
the previous two projects dealing with a similar themes. Although I�d
like to believe it, I�m not at all convinced that the admonition to
refrain from the bad mouthing held sway with the zealots. That group
consistently espouses the absolute need to maintain the status quo of
Drake equipment and nothing will keep them from venting. Basically, my
feeble request was only rhetoric and offered no tangible consequences if
one elected to ignore me and send along verbal barbs and epiteths.
Quite surprisingly, the anticipated negative responses and over-reactive,
often foul email posting, never materialized. Not a single comment that I
received could be construed as somehow impacting on someone�s root
canal nerve to some degree that would engender a response! Amazing! On
this go around, there were the usual positive comments and even several
Drake owners who volunteered to handle the adverse feedback in the event
the situation arose where I would be in need of assistance in responding.
Very thoughtful of them and much appreciated! One interesting comment was
received from a gentleman who confessed that he was in that initial
group of �rock throwers�. In the interim period, he had apparently
re-evaluated his position and offered sincere apologies for his
unsolicited, out of hand, and thoughtless remarks. To my mind, it was a
most sincere and humbling gesture and one that few individuals would
ever admit to. We chatted, became friends, and readily accepted each
other�s perspective. That bit of levity aside, let�s move on with the
more pressing details of this project.
I had stated categorically, that I probably would never undertake a
similar project based primarily on the amount of work involved in getting
the last amplifier up and running. However, in hindsight the project was
indeed psychologically uplifting . I realized subsequently that many of
the tasks undertaken that made it labor intensive could be eliminated
with some simple modifications to the process. I guess there�s something
to the adage that we �grow up to soon and smart too late�.
Additionally, higher levels of output could be easily achieved as
result of some power supply redesign including the choice of a higher
output plate transformer. The last project netted 1800 watts output.
That�s formidable and respectable in any format. However the yarning for
squeezing out an additional 400 watts was more than sufficiently
motivating. Notwithstanding the circa 1975 Drake L4B design as it
related to the early FCC restrictions as to power output, I decided
almost immediately on another attempt to approach new heights in L4B
performance with a relatively simple �supercharging� process. However,
what continued to offer almost insurmountable difficulties was the
inability to locate clean L4B�s without power supplies. It�s simply
impossible to achieve high power levels with the stock supply.
Understandably, the vast majority of radio amateurs are reluctant to
give up a fully operational Drake. That was frustrating and caused me
to work the project backwards with the building of the power supply
first. The rationale was that I could always use a big gun supply even
though the Drake L4B might never forever remain elusive. Here�s one of
those time savers I spoke about. The last time around, I built the power
supply enclosure myself. It required the work of a metal smith and worked
out to be time consuming and very expensive. On this occasion, I took a
more pragmatic approach and tried out the idea at the Timonium, Maryland
ham fest. I would look for a vintage piece of gear in a suitable
enclosure that could easily be reconfigured to suit my size
requirements. Why reinvent the wheel! There was an abundance of empty
steel cabinets but generally they were too large and for the most part
unsuitable. Fortunately, I located a circa 1959 Hewlett Packard
frequency generator lying amongst several other pieces of dated test
gear. When I inquired about price from the bedraggled vendor, I was
subject to a litany of superlatives about the nature of boat anchor
gear. Utilizing a universally understood gesture, I held up my hand,
palm out, to signify that he need not waste any more breath. I explained
that all I wanted was the cabinet. As it turned out, it was just what I
needed. It was louvered, sufficiently large to house the Hipersil, and
made of aluminum for easy cutting. $5.00 did the trick and off I went to
the car subjecting myself to the possibility of a hernia from the
weight. Most of the innards were junked even though I marveled at the
mastery of the machining of pulleys and pistons utilized to generate
stable signals. After hours of disassembly, I ended up with a bushel
full of hardware, knobs, tube sockets and all kinds of precision
resistors that were added to my junk box. In it�s original form, the
style and design of the cabinet resembled an animal carrier with a
handle at the top. In the original HP design, the chassis was mounted
vertically on the rear panel and the entire unit could be slipped out of
the enclosure. For my purposes, I stood the unit on end with the chassis
now sitting horizontally as the base and measured the height I needed to
clear the transformer. I cut off about 8-10� of cabinet height, a
corresponding length off the four interior framework supports moved the
strap to what now became the top. That completed, I was ready to go. All
I needed was a plate for the bottom on the chassis. Since I�ve gotten
the 4000VDC @ 2 amp rectifier board, complete with filter caps, bleeders,
and diode modules down to 6x8�, I really didn�t need too much additional
room. A couple of primary contactors, a 10 second mechanical delay start
relay, a mini computer fan and two meters completed the line up of
parts. 220VAC was wired directly to the power supply and dedicated solely
to that part of the project. A 115vac control voltage is brought down
from the deck to activate the solid state 180 second delay timer on
start up. After the delay, voltage is passed on to the contactors, step
start relay and then to the plate transformer. A half power switch
position was built into the supply circuitry as well as an additional
switch control to bump the primary voltage up a tad adding an additional
200 VDC. Take a look at the digitals to see what resulted.
Preparing the RF Deck
The work began with the usual stripping out of those extraneous Drake
components. Tubes, chimneys, and tube sockets were removed. Out came the
ALC board, front panel ALC switch, HV and parasitic choke assembly, and
fan. A great deal of work was eliminated when I decided not to use the
OEM Drake filament transformer. Although the 5vac rating is OK for the
upgraded tube, 30 amp capacity is a bit too high and results in
insufficient voltage draw down when using the 8877. Since tube life is
diminished exponentially with filament over voltage, I purchased the
exact rated transformer and obviated the need for a small rear panel
mounted Variac controlling the input voltage. Didn�t need the pin outs
either. Lots of work eliminated in this step alone with no compromise in
performance. A brand new 115vac line was brought into the deck and wired
to the terminal strip. A fuse was added to the line. One half of the
front panel on/off switch controls the on/off function. Since this Drake
came without a power supply, I really didn�t know what exactly was
working with the unit. That led to an interesting problem. I rewired
the amber front panel light to glow on start. No problem there. I
replaced the front panel push/pull ALC switch with a rotary 2P2T mini
switch designed to control both the amplifier standby (interrupting the
relay line) and to power up the red lamp signifying that the amp is in
the circuit. Tested out the new wiring and discovered that there was no
red light! I figured I did something wrong. Checked and checked but no
luck. There were no wiring errors. Decided to run a 115vac hot lead
directly to the lamp terminal strip. No light! Unbeknownst to me, the
lamp apparently had been smoked in its previous life. What a bummer!
Everything up to that point had been perfect with the amp so I assumed I
was at fault. Now what? There are no replacements available for this
unit at any place for any price. I anticipated a crisis of epic
proportions since I was intent on keeping the exterior of the Drake OEM
in all aspects. In desperation, I lopped off, guillotine style, the
back end of the lamp assembly, removed the two wires, the charred neon
and resistor but leaving the bezel and red lens intact. With a little bit
of grinding with a Dremel, I force fitted, from the rear, a Radio
Shack� 110vac red panel lamp into the open end of the Drake assembly.
What I initially considered a disaster of biblical proportions was
averted with a bit of expediency; and off I went once more on my merry
way. To block off the two 3-500 socket holes I fashioned a piece of
aluminum (left over from the Hewlett Package cabinet cut down) and fitted
the 8877 air system socket to the chassis utilizing the blocked opening
closest to the deck�s front panel. I made certain that the socket was
orientated in such a manner to ensure that the existing wires from the
bifilar choke would reach the filament socket pins without any
modifications. Made that error the first time around. A custom wound
1x6� porcelain HV plate choke was mounted horizontally from the chassis
behind the front panel and positioned with clearances to prevent HV arc
over and the need to keep anode wiring to a minimum. I wind these units
with #20gauge enameled wire to handle the anticipated high current. Other
incidental mods included the installation of a standard RCA jack in place
of the two pin relay control plug and the addition of a small transformer
powered 26VDC power supply for the vacuum and bias control relay. As of
this writing, this is about as far as I�ve gotten. The installation of
several additional accessory items will be addressed in the next
episode.
PS: since this was written, the Millen socket has been repositioned on
the rear panel and the HV lines installed with all parasitics.
Everything on the upper deck is about completed.