[R-390] Thinking of Nolan Lee

Don Heywood wc4g at knology.net
Mon Sep 26 15:19:39 EDT 2005


Below is one of the typical posts from my friend Nolan. I think we all
enjoyed his posts and writing ability.

73,   Don WC4G
(May 1999)
I've had a couple of requests for the list of items I did when I went thru
my EAC last year so I'm reposting my original message on it to the list. The
EAC has been running 24/7 since October of last year and I have no
complaints. I've been wanting to pull it out of the rack and do a "visual"
of it and check the tubes and the alignment but haven't had the time. Maybe
this Fall. Your mileage may vary

 nolan
-----snip from Oct 1998----- Well, after spending months slowly going thru
my two R390A's, one is finished. Below is an outline of the steps that I
took during my overhaul. This was probably one of the more evolved R390A
"overhauls" done in the South. The other, will take longer, I'm probably
going to replace all of the bushings in the RF deck among other things that
I didn't do with this one. The victim: I started with a cherry 1967 EAC
contract model that was the "lowest mileage" R390A I've ever seen. All of
the original modules, meters, covers, etc. were still on it. In addition,
all of the tubes in it had date codes within a two or three month period of
each other in 1968. Even with clean gears, there wasn't even a hint of a
wear pattern in any of the gears and all of the aluminum finish in the
tracks on the RF deck was still intact. The green paint on all of the module
hold down screws was even 100%. I'd be surprised if this thing saw more than
a few hours operation after the burn in period. There's no diode load hole
in the front panel or adjustment hole in the top dust cover for the meter
adjustment. Jerk all of the modules out of it and rip it's gizzard out and
scatter and toss the parts around! I tried, but I managed to not loose any
of the parts and didn't even have any extra ones left over. Chassis: Tested
the dial lamps, checked the value of all of the resistors, the diode, the 2
capacitors, the meters, tested the selenium rectifier, and the antenna relay
and inspected the contacts in the relay. Verified function of the main power
micro switch, it's placement, and measured the resistance of it. Measured
the resistance of all of the front panel switches and potentiometers, and
very lightly lubed the shafts of each, checked the ovens switch, verified
the values of the fuses, checked their resistance, replaced one of the fuse
holders that I didn't like the look of with a NOS one, and replaced the rear
panel IF connector, the center terminal was missing. Checked the line
filter, and checked the tightness on all of the screws holding the whole
damn mess together. I removed all of the knobs and inspected and lightly
lubed the set screws. Also verified that the index washers were installed in
the two big knobs that prevent the clamps from turning. The next step ate up
a lot of time. I removed all of the hoods of the chassis connectors to
inspect and then measured the resistance of EVERY damn wire in the chassis.
Then I installed a NOS military 3 wire 8 foot rubber 16 gauge power cord
with a molded plug. Nice and flexible SJ. The original strain clamp for the
cord was still there. First one I've ever seen. :-) Power supply module:
visual inspection, resistance readings of the transformer windings, and
wiring, inspected the solder connections, verified 115 volt setting, stuffed
two new 26Z5W's in it. Checked all of the screws and nuts for tightness.
PTO: Why bother? Chunked it in the R390A parts pile and installed an Army
rebuilt Cosmos that I've been sitting on for about ten years, sealed in the
box, to replace the Cosmos that was in there. It turned out that the
endpoint was out a little less than 2 KHz, and linear within a little less
than 200 Hz across the spectrum. I don't know what the specs on it where
when it left their hands in Feb. of 1984 but it sure aged well. :-) I guess
that I'll let it run a few weeks and then adjust the endpoint. I did power
up the oven and verified that the thermostat worked, measured the resistance
of the transformer, and tested the tube. I like the Cosmos PTO's. That blue
label sure is pretty, bubba! On a side note, I probably use a bit more
complicated method than most people do when fitting a PTO to a receiver. If
you're going to do it right, it might as well be done right the first time.
Both halves of the oldham coupler should be perfectly parallel to each other
and the centerline of both shafts should be perfectly in line with each
other on both planes. I only spent about an hour adjusting the position and
height of the PTO in the chassis, but spent several hours measuring the
components and setting up the fixtures to measure other aspects of the
components. I first measured the run out of each half of the couplings while
installed on their shafts. The one on the PTO was true within .001. The one
on the KHz shaft of the RF deck was machined improperly. he rib was .003 off
to one side and wasn't square with the bore either. I tossed it and pulled a
few others out of spares. It took several before I found one that was square
with the bore and only had a little more than 0.001 run out. The next step
was to check the center section. The width of the two groves seems pretty
consistent, but I was curious if the two groves were machined at exactly 90
degree angles to each other. The groves were of a dimension that I didn't
have any key stock for so I used two 12" long pieces of 1/4" ground steel
rod. I centered the two pieces of rod, lengthwise, one in each of the two
grooves, clamped the three pieces together. Then by measuring and comparing
the distances between the four rod ends, I could determine the exact angle
that the grooves were from each other. This part of the process was a wasted
effort, the coupling center piece from the EAC was 90 degrees like it should
be and so where the ones in spares that I checked. When I finally assembled
the receiver and physically aligned the PTO to the chassis, mechanically and
electrically, the dial indicator measured a total movement in the center
section of the oldham coupling of .003 when the KHz knob is turned. Close
enough! Put that spring on! Oh, I used a little dab of Penzoil wheel bearing
grease to lube the coupling. It's red and contrasts, in a pleasing fashion,
the blue label of the Cosmos PTO. :-) Crystal Oscillator Module: Tested the
tube, and tightened the screws holding the tube socket to the chassis, they
were loose. Checked resistor values, transformer windings and crystals. Bad
10 MHz crystal, throw one in it from spares. Most are still on the money,
the few that are "off" are well within 1 KHz or maybe a shade more. I
decided against spending ~250 dollars on new ones. Measured the resistance
of all of the wiring and switch contacts and tested all of the fixed
capacitors and spun all of the trimmers a couple of turns. Powered up the
oven and verified function of the thermostat. Also, "timed" the two switch
bodies. They were "off" a bit. Then when thru and re tested everything on
it's underside just to make sure. I figured that anything that was a pain to
remove, I double check everything. Audio module: One of the original plug in
electrolytic caps showed signs of leaking, tossed it in the trash, installed
another one from spares. Reformed both, leakage at 50 volts over the rated
voltage was less than 1 ma. per section after reforming. I fused them and
ran them for a couple of weeks at full rated voltage on one of the HV
supplies, they didn't explode and leakage declined even further. Good
enough, bubba! (yeah, I know, Doc, but the power factors were good, I even
checked that. :-) Ripped all of the paper capacitors out of the module, and
tossed them in the trash. Installed two new .022 400V orange drops in the
location that Chuck likes, and NOS Vitamin Q's in the other locations. I
have the orange drops on hand and could have used them thru out but didn't
like the way they sit on the circuit board. I did use an Orange Drops to
replace the one on the chassis under the circuit board. All of the new caps
were tested for leakage at their rated voltage and tested to verify their
value before installing. Checked all of the resistors for value, replaced a
couple. Tested the mica cap, no problem there. Tested all of the tubes, they
all passed but tossed the 0A2 and stuffed a new 6626 in it's place. I don't
trust used 0A2's, had some weird problems with them. Tested the relay and
measured the resistance of the wiring, the chokes, and the transformers. I
left the 800 cps filter alone. Probably not a whole hell of a lot of R390A's
out there that still have their original 6AK6's. All of the tubes are
original except the rectifiers and the regulator. :-) IF Module: Tested the
tubes and the 3TF7. Measured the resistance of the wiring, the transformers,
the switch contacts, and the resistors. I replaced more than a half a dozen
resistors that were out of spec. Checked the capacitors and resistors inside
the IF transformer cans, that could be tested. Some could not be tested in
circuit. I tested the big above chassis oil filled capacitor for leakage and
value. Tested all of the mica capacitors for leakage and value and then
ripped all 18 or so of the axial lead paper capacitors out of the module and
tested them just for kicks. EVERY "brown beauty of death" tubular capacitor
that was in it leaked like hell and a good percentage had microscopic cracks
in the bodies within maybe .020 of the seams and paralleling them. Most of
these caps leaked at voltages below 50 volts when tested. Only one of the
metal can axial capacitors leaked when tested. I replaced all 18 of the
capacitors with Orange Drops. For the .1 and the .033 values I used 400VDC
rated ones and for the .01 values, I used 600VDC rated ones. The reason that
I didn't use 600V rated ones thru out was their size. It was a pain in the
ass to the fit the ones that I used in there properly. If I'd have used the
600V ones everywhere, I'd have had to move the locations of some of the
capacitors and a bunch of them would have had excessively long leads. I
didn't think that this was such a hot idea in the IF section and figured
that the best placement of the parts was in the original locations. ;-)
Let's see, other than checking all of the screws and nuts, I think that was
it for the IF deck other than lightly lubricating the shaft extensions where
they passed thru the front of the IF module chassis. I didn't test the
mechanical filters. I tested the blocking cap before I tossed it and it had
tested good even at 100 volts over it's 300V rating. Whew! The last one, the
RF deck: After removing it, the first step was to take it apart. I removed
all of the tubes and tested them, the crystal oven and tested it, all of
slug racks and springs, four of which (for the variable IF slug racks) were
really weak, so I installed NOS ones in that location when I put everything
back together. The geometry for those 4 springs suck, they're stretched a
lot more than any other location. I removed all of the RF coil assemblies
and measured the resistance of all of the windings and checked what
capacitors I could. The bridge wouldn't work on some, so I kept track of
those in case I had some weird assed problem when I tried to align it later.
I disassembled the gear train and tossed all of the parts, except for the
counter, in a coffee can and sprayed a mess of gunk in there and let them
brew. They weren't really dirty, but the original lube had mostly evaporated
and what was left was stiff as hell and I don't really find the gear train
much of a mechanical challenge so I ripped it apart. About the only thing I
didn't take apart was the 6 camshafts and the antenna trimmer can. I worked
a few drops of penetrant into the bearings of the cam shafts and kept lubing
and wiping them until only clean oil would come out. Oh, I used 10W30 Mobil
1 synthetic oil for the RF deck except the detent where I used Penzoil wheel
bearing grease. Two of the cams appear to have been stamped, I guess, with
cracked dies, leaving a couple of sharp burrs on the surface that the
rollers ride on. I stoned these down while maintaining the original cam
profile. :-) When you take the split gears apart, tie them together, with a
bit of soft wire in the orientation that they were originally assembled
with. I suspect that the halves were matched. While all of the stuff soaked,
I replace the three paper capacitors, with Orange Drops, and replaced close
to ten resistors that were out of spec, checked all of the other capacitors
and found a cracked .005 1KV ceramic disc. And yes, I measured the
resistance of all of the wiring and of the band switch. ;-) I found an odd
thing. One of the tube sockets only had one screw holding it to the chassis.
When I attempted to install a screw there, it turned out that the little "C"
shaped piece of metal that curves all of the way around one side of the
socket had an unthreaded hole in it for the screw. I'm surprised that an
inspector didn't catch this at the factory. I tapped the hole and moved on.
Most of the gear clamps were either viably cracked or showed cracks when dye
checked. I guess that they must have been over tightened when it was built.
I replaced all of them with NOS clamps to be safe. I found that several of
the roller retainers had been over staked on a couple of the slug racks.
This prevented the rollers from turning. In addition, a few of then ends
were not square and had to be straightened. Burrs and gouges on the end
surfaces had to be stoned down and polished. The fit and finish of
mechanical portion of this EAC RF deck didn't impress me at all. The old
Collins decks were much more finely finished mechanically. I wiped each of
the RF cores out with a pair of damp Q-tips, wiped the slugs off, and eye
balled them. The Collins part numbers on all of the RF slugs are all the
same EXCEPT the six variable IF slugs. They are different from the RF slugs.
So, they aren't interchangeable. I assembled the RF deck and mechanically
aligned it and put the receiver back together. For what it's worth, the
repeatability of the RF slug racks averages about .001, the repeatability of
the variable IF slug racks averages .004 on one and .005 on the other. I
suspect that this could be improved upon by relocating the location of the
attachment point on the chassis of those four springs. This would require
either shorter springs or possible just creating spring "wells" that extent
slightly below the chassis so that standard RF deck rack springs could be
used. I fired it up and let it cook a while in Standby mode, at 7+000. None
of the magic smoke escaped so I switched over and set the PTO to 2455 KHz
and tightened the clamp. I stuck a VTVM lead into the unbalanced antenna
connector and cranked it down to WWL on 870 and let it run more than a day
before I did the first alignment. I always like to align a receiver twice. I
go thru it and then when I'm finished, I start all over again. I've been
playing with it for about a day and a half since the alignment. This is the
most sensitive receiver I've ever owned. It kicks ass. I did a few
sensitivity tests using my URM-25F. I questioned the results so I dug out
the URM-25D and tried them again. REAL close. I started with a receiver that
hadn't been abused and tried to do the best job that I could going thru it.
I wanted something that I didn't have to screw around with every few weeks.
Something that wouldn't wake me up at night with a burst of light like a
Romulan disrupter (I've had R390A's do that before). Something that would
sit there and run for month after month and need nothing but tube and dial
lamps like my R-1051B's. Hopefully, this will do that. Many of the of the
steps that I took, were "over kill", but I had fun doing it and learned a
few more things. The numbers you ask? Lets just say that they're as good as
the best sensitivity levels that I've ever seen posted or in print on the
R390A. Numbers, that up until now, I always had my doubts about. Guess I
better feed the critters and make me a mess of grits for breakfast,

nolan

---If an infinite number of rednecks riding in an infinite number of pickup
trucks fire an infinite number of shotgun rounds at an infinite number of
highway signs, eventually they will produce all of the world's great
literary works in Braille. --- 



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