[Milsurplus] GO-9 Project; "Which way did he go, George?"
David Stinson
arc5 at ix.netcom.com
Sun Oct 27 13:18:18 EDT 2019
Got the decks cleared of the BC-669 and the RAK/RAL projects, so it's
time to start the "Winter Hair-Puller," the GO-9 transmitter. As we saw
before, the power supply is almost completely stripped and an 813
shoe-horned in where an 803 should be nesting. The power supply and
transmitter display the sad and regrettable fate that awaited 90% of
"conversions:" a lot of wire-cutting and gutting which was not
finished- the poor thing never having done another "dit" from the time
it left Service until now, whereupon the "convert-er," converted a
beautiful piece of engineering into a corpse on the junk pile. It's
not all bad news; the transmitter came with the shock mounts, which is
great because without them, there are things on the bottom of the
transmitter that would be easy to break (not every engineering decision
is a good one). A stripped 800Hz power supply is a perfect excuse to
build a 60Hz supply, so we don't have the 800Hz boogie-man to whip.
Here is a simplified schematic of the transmitter for those who wish to
follow the discussion:
https://photos.app.goo.gl/Z3sLRrEWgFRpUtVaA
We'll start by surveying and trying to understand the changes made to
the rig, so "Which way did he go, George?" starting with the
almost-a-power-supply. It's nearly stripped and a start made on a
filament supply deck. A large transformer supplied 10VCT for the 813.
Two small ones were each 7.5VAC, wired in series to provide 15VCT,
intended for the 837 MO and 837 IA. A bunch of big mystery resistors
here and yonder. I decided to "begin at the beginning" and removed
almost all the original and "conversion" parts, leaving us a
nearly-clear cabinet in which to build our supplies, controls and
modulator. As it turns-out, our "converter" did put some thought into
the changes he made to the transmitter itself, if one assumes he did not
have access to an 803. The 813 is wired in such a way as it would
work. The 813 socket is larger than the intended 803 socket, so the
socket mounts had to be warped a bit to fit it. He did power the
transmitter up at some time, because the 813 is shorter than the 803,
the plate lead touched a ground point and arced to ground at that
point. Insulating varnish on the wire and the ground point (just in
case) addressed this. The original .01 uFd screen bypass capacitor is
missing and a large mica 600 pFd capacitor mounted to a small drill
hole. No idea why on that one. Reference the grid circuits of the
three tubes. Through pin 17 of the connection between the Transmitter
and Power Supply chassis, relay K201 closes the MO/IA gird circuits to
ground during keying. The original modifier lifted the grid circuit of
the PA from ground at the bottom of meter M302 and connected this point
to pin 17. This allows the used of grid-block keying for the
transmitter. I may retain this, since the thought of the PA producing
waste heat and running the filament-life clock, being unbiased during
key-up, is unacceptable to me.
The "Filament Resistor" Question.
As you remember, we discussed reasons why a 4.5-Ohm dropping resistor
was in the filament lead to the Intermediate Amp. After some
investigation and insights from our membership, the answer is the IR
drop in the two .5 mH chokes in the filament leads of the MO.
https://photos.app.goo.gl/5dEd6kpZZ9Bg8wA19
R-312 is included to equalize the two IR drops, which is then made-up by
supplying about a higher voltage to the MO/IA filament buss. To get
12.6 V to the tube filaments at 60 Hz, one must supply about 15.5 VCT to
the buss. While 15 VCT transformers can be found surplus, one of my
goals in doing this work is the hope that others will get their rigs off
the garage floor where it's sat for 40 years and breath life back into
it. Really didn't like the idea of using a non-standard transformer.
There are a lot of 12VCT, 3 Amp transformers out there. Radio Shack
used to sell them by the basket and you see them at hamfest for a couple
of bucks all the time. So began looking for another solution. Here is
a photo of the MO stage. The two filament chokes, wound basket-weave on
a wooden core, are easy to see on the right:
https://photos.app.goo.gl/gRbTQGYbwVE7zHqT6
Modern ferrite-wound chokes can deliver significant inductance without
large IR loses, so I decided a non-destructive solution was to bypass
these two chokes with ferrite-loaded coils and bypass R-312, allowing
standard 12.6VCT supply to the MO/IA filament buss. R312 is the center
of the three clip-mounted resistors:
https://photos.app.goo.gl/YQsntABB46pMorJRA
https://photos.app.goo.gl/GsoKN6iTZ9pqhBVQ6
https://photos.app.goo.gl/b7ncNWyhQhtt669XA
Replacing the 813 with the correct 803 hit a small snag; the 803 socket
I had was the same size as the 813 socket- too big. Luck was with me,
because I'd acquired a fried-transformers GP-7 transmitter at HamComm
many years ago to keep as a parts donor. It had the correct, smaller 803
socket, but there was yet another catch. There had been arcing around
the socket ( high power at alititude? ) and there were nasty carbon
tracks between the filament tubes and from filament to the screen pin.
Cleaning didn't touch them. Used plumber's emory cloth to remove the
tracks completely, then covered the areas with a good coating of High
Voltage Insulating varnish:
https://photos.app.goo.gl/niUjad3wVDQAGaLQ7
The 803 was originally mounted with rubber grommets at each of the
mounting screws. The old ones were long gone and the ones from the GP-7
parter were crumbling and unusable. Did some searches and asked a local
car mechanic if hi-temperature grommets were available. Nothing I found
was satisfactory. Decided to go with silicone faucet washers (that
might come back to haunt me, HI). They were slightly too large,
preventing the tube from seating the last 16th of an inch or so, but
that doesn't seem to have been a problem. In fact, it might be a
positive as this will allow air flow under the tube.
https://photos.app.goo.gl/ULsbPa295Q5DG8Bn9
The original screen bypass cap was missing and a "tacced-in" 600 pFd
replacement installed. I removed this cap and installed a .01, 1000V
ceramic disc.
https://photos.app.goo.gl/fT61C5rcthXsDjm3A
After the filament circuit changes and replacing the 803, I decided to
run a first test at low voltages. Supplied 420 VDC to all High Voltage
busses. The rig took right off and produced 15 W out with clean
grid-block keying. We'll call this "prototyping" because "haywiring"
(a.k.a. "the truth") sounds so... yeah. That:
https://photos.app.goo.gl/TTm68nZ2YEApKvr96
Still much to do. BIg power supply build ahead. Fitting the
transformer deck:
https://photos.app.goo.gl/f4sfAcDb5eciFZjB9
The big black transformer is 1200VCT, which with a bridge rectifier
should deliver about 1700 VDC to the 803. The "Economy" center tap is
too "hot" for the Low B+ to MA/IA at 800+V, but I have a series cap to
tone it down a bit, followed by a MOSFET regulator to fix this buss at
525V. We'll see how it goes.
TNX OM ES 73 DE Dave AB5S
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