[Collins] PM-2 Replacement transformer project
wabate
wabate at verizon.net
Mon Apr 26 11:42:56 EDT 2010
PM-2 Replacement transformer project
From an aesthetic and compactness standpoint, I prefer the PM-2 power
supply to the 516F-2. But the PM-2 has that limitation of intermittent
operation, whatever that means. I was not able to find any
documentation on how intermittent was defined. Apart from the obvious,
that RTTY is ruled out, what would be the limitation for audio
compression? How about continuous SSB or CW operation in a contest?
This was enough to make me look at transformer design in an effort to
remove that limitation. The good news is that wire insulation has
improved dramatically in the last 50 years or so. An unexpected (for
me) advancement was in transformer iron that leads to increased
efficiency and better magnetic properties. After much what ifs and
juggling of parameters, a new transformer design was established that
met my goals.
So what’s out and what’s in? Well I dumped he 400 HZ specification.
Figured I could live without that! :) I also thought 220 VAC operation
had limited appeal, so the dual primary got dumped. What I got was a HV
primary that was rated for continuous operation. My PM-2 measured 833
VDC @ 240 ma. I can’t figure that out based on the Collins spec of 700
VDC, even with 120 VAC in a 115 VAC primary. Well I liked more voltage
on the plates anyway. So the new transformer had that voltage spec.
The low voltage and filaments spec stayed the same.
First I tested the original PM-2 with resistor loads (I was not about to
rum the KWM-2A at key down as a guinea pig!). The closest resistor
values I had put a 240 ma load on the high voltage (833 VDC), 293 VDC at
210 ma and 6.3 at 12 amps. This exceeded the original specs slightly.
I placed a temperature probe inside the windings and on top of the
laminations and turned on the supply. After 25 minutes I had a
temperature inside the transformer of 136 F and the laminations
temperature was 131 F. I stopped at 25 minutes as the temperature
appeared to be taking off.
Next I wired the replacement in and ran the same test. I had 860 VDC at
240 ma, 288 VDC at 187 ma and 6.3 VAC at 12 amps. I could not insert
the probe in the same winding location so I did not measure winding
temp, just lamination temperature. It took 1 hour of operation to get
to the same 131 F that the original reached in 25 minutes. So far, so
good. After 2 hours and 45 minutes of continuous operation, the
lamination temperature rose to 167 F. At that point I felt I was
reaching equilibrium and felt nothing else was to be proven. No moke or
burnt insulation smell either. The specifications on the new
transformer wire is a rating of 150 C! The insulation is rated at 130
C, so you see we are no where near the ratings even at continuous duty.
Now there was one concession in the design. I had to accept a slight
lamination thickness increase. But the transformer still utilizes the
same mounting holes. No Drilling! I did raise the transformer off the
chassis just to make sure there would be no interference with the wiring
grommets. That’s it! I’m happy. I want to tweak the windings a little
bit to lower the HV but I think that will be it. Production costs are
estimated at about $125 plus S&H. So is there any interest out there?
I would coordinate the project and handle the paperwork. All those that
are interested would have to do is write a check. What we would get is
a 516F-2 in a PM-2 package! And if you let your imagination run, you
will realize that you can install one of these transformers in a burnt
out 516F-2, eliminate both rectifier tubes and two chokes and have a
resurrected 516F-2. Not too shabby.
If we get enough people to sign on, the cost might lower. So let me
know if you are interested. Please email me direct and I’ll get back to
you. I’m a few weeks away from solidifying things.
73,
Bill, K3PGB
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